Blog Search

Boeing Silences Wistleblower

A former Boeing quality control manager has been found dead in his truck outside of a Charleston, South Carolina hotel from a reported gunshot wound days before he was due to provide evidence in part of an ongoing whistleblower lawsuit against the Arlington, Virginia-based aerospace giant.


“John Barnett, a former Boeing employee who had reportedly raised concerns about the company's production issues, was found dead of an apparent suicide, according to authorities in South Carolina.



Barnett had worked at Boeing for 32 years before leaving the company in 2017, according to the BBC, which previously reported on his efforts to raise issues about the company's production issues.


The 62-year-old died of a self-inflicted gunshot wound, the Charleston County coroner's office in South Carolina confirmed on Tuesday. The Charleston City police are investigating, the coroner's office said, without giving any other details.


Barnett was in the middle of a deposition in an ongoing whistleblower retaliation case against Boeing, according to a statement from his attorneys, Robert Turkewitz and Brian Knowles.


‘He was in very good spirits and really looking forward to putting this phase of his life behind him and moving on. We didn't see any indication he would take his own life. No one can believe it’, they said.


Barnett was a quality manager at Boeing. He had ‘exposed very serious safety problems with the Boeing 787 Dreamliner and was retaliated against and subjected to a hostile work environment’, his attorneys said.


Boeing, in a statement, said: ‘We are saddened by Mr. Barnett’s passing, and our thoughts are with his family and friends’”. -Reuters


Curiously enough, on the same day the whistleblower was discovered dead, The New York Times reported that the U.S. Federal Aviation Administration identified dozens of quality-control failures throughout Boeing’s 737 MAX 9 manufacturing process in its safety audit, which occurred as a result of a door panel that blew off a 737 Max 9 during an Alaska Airlines flight on January 5th.


“A six-week audit by the Federal Aviation Administration of Boeing’s production of the 737 Max jet found dozens of problems throughout the manufacturing process at the plane maker and one of its key suppliers, according to a slide presentation reviewed by The New York Times.


The air-safety regulator initiated the examination after a door panel blew off a 737 Max 9 during an Alaska Airlines flight in early January. Last week, the agency announced that the audit had found ‘multiple instances’ in which Boeing and the supplier, Spirit AeroSystems, failed to comply with quality-control requirements, though it did not provide specifics about the findings.


The presentation reviewed by The Times, though highly technical, offers a more detailed picture of what the audit turned up. Since the Alaska Airlines episode, Boeing has come under intense scrutiny over its quality-control practices, and the findings add to the body of evidence about manufacturing lapses at the company.


For the portion of the examination focused on Boeing, the F.A.A. conducted 89 product audits, a type of review that looks at aspects of the production process. The plane maker passed 56 of the audits and failed 33 of them, with a total of 97 instances of alleged noncompliance, according to the presentation.


The F.A.A. also conducted 13 product audits for the part of the inquiry that focused on Spirit AeroSystems, which makes the fuselage, or body, of the 737 Max. Six of those audits resulted in passing grades, and seven resulted in failing ones, the presentation said.


At one point during the examination, the air-safety agency observed mechanics at Spirit using a hotel key card to check a door seal, according to a document that describes some of the findings.


In another instance, the F.A.A. saw Spirit mechanics apply liquid Dawn soap to a door seal ‘as lubricant in the fit-up process’ according to the document. The door seal was then cleaned with a wet cheesecloth, the document said, noting that instructions were ‘vague and unclear on what specifications/actions are to be followed or recorded by the mechanic’.


Asked about the appropriateness of using a hotel key card or Dawn soap in those situations, a spokesman for Spirit, Joe Buccino, said the company was ‘reviewing all identified nonconformities for corrective action’.


Jessica Kowal, a spokeswoman for Boeing, said the plane maker was continuing ‘to implement immediate changes and develop a comprehensive action plan to strengthen safety and quality, and build the confidence of our customers and their passengers’.


In late February, the F.A.A. have the company 90 days to develop a plan for quality-control improvements. In response, its chief executive, Dave Calhoun, said that ‘we have a clear picture of what needs to be done’, citing in part the audit findings.


Boeing said this month that it was in talks to acquire Spirit, which it spun out in 2005. Mr. Buccino said on Monday that Spirit had received preliminary audit findings from the F.A.A. and planned to work with Boeing to address what the regulator had raised. He said Spirit’s goal was to reduce to zero the number of defects and errors in its processes.


‘Meanwhile, we continue multiple efforts undertaken to improve our safety and quality programs’, Mr. Buccino said. ‘These improvements focus on human factors and other steps to minimize nonconformities’.


The F.A.A. said it could not release specifics about the audit because of its active investigation into Boeing in response to the Alaska Airlines episode. In addition to that inquiry, the National Transportation Safety Board is investigating what caused the door panel to blow off the plane, and the Justice Department has begun a criminal investigation.


During the F.A.A.’s examination, the agency deployed as many as 20 auditors at Boeing and roughly half a dozen at Spirit, according to the slide presentation. Boeing assembles the 737 Max at its plant in Renton, Wash., while Spirit builds the plane’s fuselage at its factory in Wichita, Kan.


The audit at Boeing was wide ranging, covering many parts of the 737 Max, including its wings and an assortment of other systems.


Many of the problems found by auditors fell in the category of not following an ‘approved manufacturing process, procedure or instruction’, according to the presentation. Some other issues dealt with quality-control documentation.


One audit dealt with the component that blew off the Alaska Airlines jet, known as a door plug. Boeing failed that check, according to the presentation. Some of the issues flagged by that audit related to inspection and quality-control documentation, though the exact findings were not detailed in the presentation.


The F.A.A.’s examination also explored how well Boeing’s employees understood the company’s quality-control processes. The agency interviewed six company engineers and scored their responses, and the overall average score came out to only 58 percent”. -Mark Walker, New York Times